Improvement Work Method for Defect Reduction in Marking Brake Pad Process

DOI: 10.14416/j.ind.tech.2020.08.004

Authors

  • Saran Narkbovornwijit Field of Engineering Management, Department of Industrial Engineering and Management, Faculty of Engineering and Industrial Technology, Silpakorn University
  • Prachuab Klomjit Field of Engineering Management, Department of Industrial Engineering and Management, Faculty of Engineering and Industrial Technology, Silpakorn University

Keywords:

5W1H; ECRS Principle; Hypothesis Testing; Payback Period

Abstract

Brake pad manufacturing found the incorrect position of text on brake pad defect in the marking process 10,976 pieces per day or 81% of the daily production plan and caused defects from 10 models. The temporary solution of the company before investigators studied process shown that provided an operator to arrange brake pad rows on the conveyor before pass the marking machine so caused to hire the operator. Investigators studied the work method by flow process chart, analyzed the value of activities, queried 5W1H shown that the main cause of the defect was inappropriate designing the conveyors in the process then applied ECRS principle to find improvement way by making new conveyors and adjusting the initial spacing of brake pad in the oven. The formula table was made by using 10 models to find the number of brake pads per row and appropriate initial spacing of brake pad to actual work. Result from statistical testing at 95% confidence level shown that adjusted the value of variables from formula table that could reduce the incorrect position of text on brake pad defect 10,976 pieces per day or 100% of the daily production plan. Besides, average capacity increased 1 piece per row and the payback period of improvement conveyors was 1.275 days.

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Published

2020-08-25

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Section

บทความวิจัย (Research article)